Dust Explosion in a Specialty Pharmaceutical Plant
(West Palm Beach, Fl) February 6, 2006 -- The explosion occurred
in a blending operation handling particulate bulk solids. Multiple
ingredients are added to a mixer manually from 50-pound sacks.
The mixer is a tumbling type multifaceted drum that is located
in a stand alone, dedicated room. The ingredients are added from
a staging area located in the room immediately above the mixer
through a port that is closed via a butterfly valve for mixing.
The rotation is quite slow and the mixer is supported by externally
mounted bearings. There is a shaker screener on the top of the
fill port. Manual additions of ingredients in small quantities,
no moving parts, external bearings, slow rotation speed, and excellent
housekeeping all support the conclusion that in ordinary circumstances
this apparatus would not be considered to be a likely locus for
a dust explosion.
Nevertheless, an explosion occurred in the mixer drum during
the addition of the last but one bag of ingredients. The explosion
developed slowly as these things go, with the initial ignition
occurring at the bottom of the drum, some 16 feet below the worker
who saw the flame as he was pouring the contents of the 50-pound
sack into it. Incredibly and most fortunately, although injured,
this worker was able to turn away in time to avoid what could
have easily been a fatal experience.
The flameball left a clear imprint on the staging room via burn
marks and heat discoloration that extended throughout the room
and out of the room via open doorways on two sides. One sprinkler
head that was above and in close proximity to the fill port opening
was knocked off the piping and this allowed water to pour into
the room. Other sprinkler heads in the room were intact, undamaged,
and did not deploy. Obviously, dust explosions happen too fast
for sprinkler systems.
Investigators found faulty bonding and grounding for the shaker
screener and for attached 4-inch diameter, wire-reinforced, plastic
tubing that was used to connect the screener to a central dust
collector. There was no evidence of flame spread propagation to
the dust collection system. Since the faulty bonding and grounding
was found above the mixer (the bonding and grounding for the mixer
drum was OK), but ignition was observed to occur at the bottom,
it was concluded that a static spark from this source would not
be a likely root cause factor in this accident.
The ingredients were sent to a lab for testing for reactivity
(Kst and Pmax), for ignition sensitivity (i.e. Minimum Ignition
Energy - MIE), and for resistivity. It was found that the material
being added at the time of the ignition had several peculiar properties:
It had low MIE (<10 mJ), high resistivity (>1010 ohms),
and a fraction of it was so fine that it behaved and looked more
like smoke than like dust. The other materials all had relatively
high resistivity values, too, which led to the conclusion that
the source of ignition was a kind of transitional bulking-brush
discharge that ignited the vapor like component of the ingredient
being added. Although, it would normally be considered to be very
unlikely that manual additions of material in the quantities encountered
in this process could be ignited via a bulking-brush discharge,
this was the most plausible explanation for this event.
Lessons learned: Care should be taken to learn of any materials
being processed that have low MIE. Generally, I suggest that any
particulate material with an MIE = 20 mJ should be carefully considered
and handled in a manner so as to guard against static ignition.
In this case, the solution included properly bonding and grounding
all equipment, and the ingredient involved was replaced with a
much less reactive alternative. Even though conventional wisdom
would suggest that bulking-brush discharge ignition would be most
likely to occur in large process vessels such as silos that are
being filled via rapid pneumatic conveyors, care should be taken
to recognize that even smaller quantity operations, with manual
filling can lead to trouble for materials that have both high
resistivity and low MIE. Although no harm came from the wire-reinforced,
plastic tubing in this incident, this material was removed and
a flex-metal duct was installed instead. Plastic tubing can generate
a lot of static and is not recommended especially when handling
low MIE dusts. Metal wire has been found to break in the tubing
and it is not sufficiently reliable or effective to bond and ground
it.
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